Showing posts with label Interior. Show all posts
Showing posts with label Interior. Show all posts

Wednesday, 3 September 2025

FHC resto nr. 171; A few rectifications


It’s six months since I last worked on the ’76 car. And as you can read in my blog, there are several reasons for this: ‘t Kreng's water pump, the work on the DHC, and my regular work of course. But with a few weeks holiday ahead of me I decided it would be nice if I could finish the rear of the car’s interior. Time to pull the cover of the car and start to work. But first there were a few (small) jobs that needed rectifying. Starting with the mounting hardware for the brake balance pressure reducing valve. While fitting the steering column I found out I had used the wrong bolt to fit the valve. It was the bolt for the column’s G-clamp, which is longer than the one for the valve. As I had prepared only one bolt of the correct length it was taken from the valve and used on the steering column. But that meant I needed to prepare new fasteners for the valve. Luckily I had a few rusty spares lying around. And with the help of a friend’s blasting cabinet, a blow torch and a small container filled with oil, it was blackened and fitted. Looks quite nice.


Next job that needed rectifying were four small holes in the cabin floor. These needed their rubber plugs fitted. Something I forgot when I fitted the sound deadening pads almost 10 years ago. First Idea was to just open up the holes and insert the blanking plugs. But that didn’t work. The combination of the steel panel, the underbody protection and the sound deadening pads was too thick to fit the blanking plugs. Time to borrow a professional (and very sharp) hollow punch set from a friend to remove the sound deadening pads around the holes. These punches are designed to cut through material when hit with a (big) hammer. Not a good idea on steel panels. But being very sharp punches, they could cut through the sound deadening by simply pushing and turning them through the sound deadening pads. This way a ring was cut loose from the sound deadening pads. And this remaining ring could then be removed quite easily using a pen knife and a small sharp screw driver. And this removed enough material for the blanking plugs to be fitted. Some clear wax oil was used for rust protection.


The last correction concerned the carpet over the transmission tunnel. When I fitted it over the 2024 Christmas period, I wasn’t impressed in the way the carpet ballooned coming down from the top of the transmission tunnel. So I decided to use some fancy high strength “gecko” tape to glue the carpet to the top and the sides of the transmission tunnel. And this worked very well. And it enabled me to perforate the carpet to fit the plastic carpet protector and the mounting bolts for the seats.


The last tasks for this productive afternoon were the preparations for mounting the parcel shelf. A job I've been putting off for a while now, because I'm afraid I'll make a mistake with the dimensions for the holes I need to drill. Measure three times, drill once! The fact that the guy who covered the parcel shelf has died since he delivered this quite nice job, didn’t help! Also checked and corrected the sound deadening panel I made and which fits between the parcel shelf and the rear window. More on that later!



Sunday, 17 August 2025

More TLC for ‘t Kreng


Part two of the general service and maintenance check of ‘t Kreng, which was carried out over this weekend. With the most important job being flushing and bleeding the hydraulic fluids. From a mileage point of view this wasn’t really necessary. But both clutch and brake fluid were well over three years old. Where my normal interval for these fluids is two years. So time to call on the help of a friend for a traditional flushing and bleeding session!
Starting with emptying and cleaning the clutch cylinder’s reservoir. And this immediately showed why regular hydraulic fluid changes are absolutely essential. The fluid I sucked out of the clutch cylinder’s reservoir was almost completely black. Forgot to take the picture but the one in this earlier post gives a good indication on how it looked! After that the reservoir was cleaned and filled was fresh brake fluid (Bosch DOT4). Flushing and bleeding the clutch system was left till later though.


We moved to the brake system instead. Starting with the removal of the brake master cylinder’s pressure failure switch. Always tricky as this one is by now old and brittle. But I succeeded to remove it intact. Probably helped by the anti-seize paste I used when I re-fitted it a few years ago.


With that hurdle successfully out of the way, we could start flushing and bleeding the brake system. Starting with the front brakes which are fed through the rear chamber of the fluid reservoir. This chamber was also first emptied with a small manual suction pump, after which it was filled with fresh fluid. And the flushing/and bleeding could begin, starting with the front calliper on the right hand side. For both sides together, we used twice the contents of the rear chamber. No air came out.


As the reservoir’s front chamber can’t be emptied with my simple pump (a large syringe type affair) we had to empty this chamber by pumping the brake pedal with one of the bleed nipples at the rear open. My assistant was a bit overzealous though, emptying the front chamber too far. Which resulted in some air being drawn into the system. Luckily the air could be bled very easily though one of the two bleed nipples at the back.


Next job was flushing the clutch system. With the reservoir filled with fresh fluid, and the old fluid still in the pipe, it should be clearly visible when all the old fluid was expelled from the system. It was! But just to be sure all the old fluid was expelled, the contents of a full reservoir were flushed through the system after clean fluid came out of the master cylinder. Job done! Actually the biggest problem here was removing the rubber dust cap from the slave cylinder’s bleed nipple underneath the car! It had collected some oil, resulting in a rather slippery dust cap.


Next on the to-do-list where the wheels. They would certainly benefit from a good clean. Rather straightforward with warm soapy water and a collection of different brushes. I did need a shower afterwards!


Final job on the on the to do list was cleaning the two earth points behind the head lamp mounting panel. Hardly any oxidation there, only a lot of paint. So I cleaned away the paint around the mounting points and refitted the earth points using some copper slip to prevent future corrosion.


And the final job for the day was cleaning the steering wheel and treating it with a leather conditioner. The lack of use in the recent years had dried out the steering wheel’s leather cover. And after well over thirty years of service (it started life with me when I fitted it to a Mini Cooper, in 1994!), it could do with some tender loving care. It did soak up quite a bit of leather conditioner fluid.



Sunday, 9 February 2025

FHC resto nr. 168; A few small jobs

Over the weekend I spent some time in the shed. Mostly to do some work in preparation for the repairs of the DHC (more on that later). And in between I carried out a few small jobs for the ’76 car. Starting with the gear lever gaiter. This was refurbished over 10 years ago, but it was still missing the top finisher. This part was 3D printed already 4 years ago but I never got round to fit it. But that is sorted at last!


The next job was to trial fit a new reverse light switch. As the original items have the wires fixed permanently they are becoming prone to failure with age. This is caused by the aging wires breaking of where they are soldered to the switch. And the original switches are no longer available. So I went in search of an alternative, which I found in the parts list for LT77 equipped Land Rovers (part number PRC2911G). And as you can see it is a perfect fit. Now I only have to fabricate a short loom with two spade connectors on one end and a two pin super seal connector on the other end. Spot the difference!



It looks like old oil and grime is coming to the surface of the alloy casting!

And final job should have been fitting the mounting tube and bearing carrier for the steering column. But an inspection before started work revealed some serious distortions of the mounting tubes for the column switches’ shroud. Probably caused by excessive temperatures during the paint removal process (pyrolysis). So another job that is added to the to do list (cleaning and painting the sourced item from the shed.



Sunday, 19 January 2025

FHC resto nr. 166; Interior light


Or small steps at a time, to get the ’76 car finished! Several years ago I spent some time cleaning this early roof mounted interior light, which I found among my spare parts. This was removed from a parts car a friend broke in 2016. The light corrosion on the metal parts is clearly visible in the pictures below



Fast forward to September 2020 and I found some time to clean the light properly. For this I used the same method as for cleaning the connectors of the various wiring harnesses. Which meant immersing the armature in a solution of rock salt, dissolved in hot water and cleaning vinegar. After leaving it in this solution for 15 minutes it was rinsed of with clean water and dried. Final job was getting rid of any remaining oxidation with an assortment of small wire brushes.


The cover was cleaned using hot water and liquid dish soap. With a final polish with tooth paste and an old electric tooth brush. And as a finishing touch I painted the outside silver, using a Tamiya paint marker.


And while I was in the shed today, to check a few things for the repairs of the DHC, I thought it a good idea to fit the interior light to the inside of the roof. Mainly because I had it in my hands for the umpteenth time! A rather straightforward job. Although I took a little extra time to make sure I had the correct location, before cutting a hole in the custom made head lining!




Sunday, 8 December 2024

FHC resto nr. 165; Restarting on the interior


It has been well over 6 months ago that I last reported any progress on this project. But with a two week break from the office scheduled around the Christmas and New Year period, it’s about time to restart work on this '76 car. First task being to make an inventory of the parts and fasteners needed to finish the interior.


And to trial fit the carpet that is going to cover the transmission tunnel. I had planned to fit it over the weekend but found out it needed a bit of trimming, but also (and more importantly) that I really need an extra pair of hands to get a decent fit of this carpet. Definitely something for the Christmas break! Though having the carpet in position gave me an opportunity to get a glimpse of the car’s future interior. Especially combined with the rear bulkhead trim panel in position!


And because I wasn’t able to finish the tunnel carpet, I decided to fit some parts that I have had in my hands far to often: The various brackets and supports for the dashboard. I was glad I had a car in the shed to use as reference, especially for the three support tubes for the steering column rail.





Sunday, 26 May 2024

FHC resto nr. 164; Trial fitting the carpets

Slowly preparing to get back to the ’76 car’s interior. As both the inner sill carpets of the custom carpet set were slightly to long, I decided to trial fit the carpet piece for the transmission tunnel. The carpet piece did fit, though a small alteration was necessary for the hand brake lever cut-out. But I also found out that the alloy extension for the throttle pedal was sitting to close to the transmission tunnel. As the pedal was rubbing the carpet, there was the risk that the pedal wouldn’t return completely when the throttle was released. Luckily there was some room for adjustment! Below two before and after pictures taken a few minutes apart. Spot the difference;



But while moving the pedal extension, I noticed a lot of light grey dust on the floor of the car. This turned out to come from the carpets backing material.


Not particularly impressed! Especially as the backing material for the floor mats that go over the foot-well carpets is made from the same material. Luckily the solution for this problem was fairly easy, a brush on rubber seal for flat roofing etc. But first I used a left over from one of the sill pieces to test it. And after drying for 24 hours it remained flexible, with good adhesion too. Mission accomplished.



But most importantly the dark sealant doesn’t shine through the light carpet material. And it will add an anti-slip layer to the back of the carpets, and maybe even a little extra sound proofing.

Thursday, 9 May 2024

FHC resto nr. 163; Spreading the load


Or strengthening the rear of the armrest. With the facia switch panel back to its former glory, it was time to switch my attention to the rear of the interior. The Armrest to be precise. For those who have owned or worked on a TR7 that has had a hard life (read careless or incompetent owners) will know that the armrest mounting points can suffer. And all armrests in my spares collection had suffered! Luckily there was one item with only
minor damage. But better safe than sorry. So I decided to fabricate a few small steel plates to go over the affected areas. The idea behind it being, that by spreading the load over a larger area, the mounting points will be more stable and further damage will be prevented.
The first stage of the job at hand was measuring the dimensions of the affected areas and putting them in a digital format.


This was than printed out in full size on paper, cut out and glued to some left over 1.30mm thick steel pieces (see picture above), to act as pattern for cutting and drilling. This gave me these three pieces (see pictures below). The first picture was taken after cutting the pieces from the steel left overs, with the remains of the pattern paper still in place. The bottom picture was taken after the paper and glue was burned away with a gas torch and the edges were finished with a grinding wheel.



And in their designed position, after adding a bit of black paint from a rattle can:

Trial fitting the two plates to strengthen the mounting points to the rear bulkhead.
One plate needs to be flipped through 180° in the picture above,
when the arm rest will be fitted to the car.

And the strengthening plate for the mounting area
where the arm rest lid is fitted to the cubby box.

Tuesday, 7 May 2024

FHC resto nr. 162; Facia switch panel finished


I left this part of the car’s restoration a few days ago with an illumination strip that needed some of the lettering filled in with paint. And after the enamel paint had hardened, the excess paint could be gently scraped off with a surgical knife. With the final job being polishing the visible transparent illumination strip. For this I used another proven method; gently rubbing toothpaste over the surface to give a smooth and clear finish.



And this brought me to the final part of this job; assembling the facia switch panel, using all previously prepared parts including the front panel refurbished well over a month ago. When it was changed from light grey to black.


The actual assembly was rather straightforward, with the most “difficult” part being the application of the black tape that is used to prevent light leaking from the bottom edge of the illumination strip. But within only a few minutes after starting the re-assembly the switch panel was finished. So to end this short post a few pictures of the finished switch panel:




Next planned job for the '76 car will be fabricating something completely different and pretty small! Oh ... and there might be an issue with ‘t Kreng’s coolant system (a leak!?)