Monday 17 September 2018

FHC resto nr. 69; Heater rebuild part 7

This should have been the final chapter of the heater rebuild! Sadly I had to take a few steps backwards. First I had to remove the back plate for the bulkhead seal from the heater unit. Not because anything was wrong with it, but because I decided it could do with some detail changes.
With the original set-up the steel tubes supply some of the rigidity to the plate to help press the seal more firmly against the bulk head. But while measuring an old seal for remanufacturing purposes, I noticed that even with the original set-up the seal wouldn't seat  properly against the bulk head!  Time for a redesign of the plates mounting, especially as the coolant tubes don't support the plate anymore, because they just pass through the original holes without any physical connection. And the plastic tabs on the heater body, to which the back plate is riveted, look rather flimsy too. This prompted me to add a second mounting bracket to the plate. It not only adds stability to the plate, it also helps with compressing the seal better!
With this part ready I used the back plate as a template to generate a DXF-file, which in turn was used by Rubberhuis Maastricht to fabricate the (cell foam rubber) seal, using modern CNC equipment. They also used this equipment to fabricated the condensation drain seal, which is fitted between the bottom of the heater's fan housing and the transmission tunnel:



Next it was time to remanufacture a new seal to go between the heaters fresh air intake and the bulk head. For this I also used cell foam rubber, a self adhesive rectangular profile of 20 x 15 mm. And with four carefully measured 90° V's cut from the seal, it could be fitted to its designated location:


With all seals ready and fitted where possible, it was time for the heater's final assembly; refitting the back plate and fitting the coolant hoses between the heater's matrix and the pipes passing through the bulkhead. At least that's what I had hoped for. Sadly even with the fairly slim heater hose I had acquired, it  was still impossible to negotiate the bends needed to fit the hose between heater matrix and bulk head passage. Especially the radius for the top hose turned out to be impossible tight for a proper fit.
Time for another step back and plan B, consisting of a stainless heater pipe assembly for the original heater layout, purchased through one of the rather reputable TR7 suppliers in the UK:


Which was duly cut down approximately in the middle of the pipes, shortening the necessary hose length considerably. But most importantly this got rid of the tight bend for the top hose, at least it should have ... The picture above does give a clue to what's the main problem. The two pipes are identical and much too far apart in the centre section. As a result of this even with the top pipe hard against the ventilator motor there still is an almost 10 mm gap between the rivet holes in the base plate and the ones on the heater's casing, not good! Luckily I still had the old pipes lying around for comparison:


Clearly visible is the difference in shape between the aftermarket stainless pipes and the original ones. And this frontal shot of the assembly clearly shows the rather poor quality of the work done by whoever fabricated it:


So instead of fitting the heater to the car I will have to adapt/prepare the original pipes and use them instead. To be continued, but hopefully not for too long!

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